ISSN 1673-8217 CN 41-1388/TE
主管:中国石油化工集团有限公司 主办:中国石油化工股份有限公司河南油田分公司
王伟, 焦广文, 欧阳文华. 1999: 交直流电脱盐技术在河南油田炼油厂的应用. 石油地质与工程, 13(06): 45-47+61.
引用本文: 王伟, 焦广文, 欧阳文华. 1999: 交直流电脱盐技术在河南油田炼油厂的应用. 石油地质与工程, 13(06): 45-47+61.
Wang Wei, Jiao Guangwen, et al. 1999: Application of A.C.and D.C.Electrical Desalting Technology in Henan Oilfield Refinery. Petroleum Geology and Engineering, 13(06): 45-47+61.
Citation: Wang Wei, Jiao Guangwen, et al. 1999: Application of A.C.and D.C.Electrical Desalting Technology in Henan Oilfield Refinery. Petroleum Geology and Engineering, 13(06): 45-47+61.

交直流电脱盐技术在河南油田炼油厂的应用

Application of A.C.and D.C.Electrical Desalting Technology in Henan Oilfield Refinery

  • 摘要: 河南油田炼油厂50万吨/a常减压装置于1992年建成,电脱业采用国产的交流电脱业设备.随着原油日益变重和含水量的不断增加,生产中脱业装工变压器跳闸频繁,影响装里的平稳操作,且脱业效呆逐渐变差,为此,1996年对炼油厂原电脱盐装置进行了交直流电脱盐技术改造.两年多的生产运行表明,脱盐脱水效果有了明显改善,达到了中石化要求的脱后食盐小于3mg/L、合水小于0.1%和污水含油不大于200mg/L标准,同时耗电量下降81%左右,不但解决了生产中存在的问题,而且创造了显著的经济效益和社会效益。

     

    Abstract: An A. C. electrical desalter was used in the 50×104t/a atmospheric decompressor in Henan OilfieldRefinery which was put into production in 1992. Desaltertransformer tripping occurred frequently during operationas heavier crude oil were used and water content in crudeoil increased, resulting in unsmoothed operation and lowdesalting effect. Technical innovation of A. C. and D.C.electrical desalting were performed in 1996. Desalting anddewatering effects were significantly improved and met thestandards of salt content less than 3 mg/l, water contentless than 0.1% and oil content in oily water less than200mg/l. In addition, power consumption lowered about81%.

     

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