ISSN 1673-8217 CN 41-1388/TE
主管:中国石油化工集团有限公司 主办:中国石油化工股份有限公司河南油田分公司
高博, 覃青松. 2011: 齐40块蒸汽驱试验区井组开发后期转热水驱研究与应用. 石油地质与工程, 25(01): 86-87+100+145.
引用本文: 高博, 覃青松. 2011: 齐40块蒸汽驱试验区井组开发后期转热水驱研究与应用. 石油地质与工程, 25(01): 86-87+100+145.
2011: Study and application of thermal recovery technology after water flooding at the late development stage in steam drive well group of test area in Qi40 block. Petroleum Geology and Engineering, 25(01): 86-87+100+145.
Citation: 2011: Study and application of thermal recovery technology after water flooding at the late development stage in steam drive well group of test area in Qi40 block. Petroleum Geology and Engineering, 25(01): 86-87+100+145.

齐40块蒸汽驱试验区井组开发后期转热水驱研究与应用

Study and application of thermal recovery technology after water flooding at the late development stage in steam drive well group of test area in Qi40 block

  • 摘要: 齐40块莲Ⅱ油层于1998年10月开展4个井组的蒸汽驱先导实验,2003年7月开展7个井组的蒸汽驱扩大实验,目前齐40块蒸汽驱试验区共有11个汽驱井组,均处于蒸汽驱开发末期的突破阶段。为了提高蒸汽驱经济效益并为工业化实施区提供后期的调整技术选择,运用数值模拟对试验区蒸汽驱后期进行了转热水驱的研究,设计了注水温度、注入速度等参数,现场应用后见到明显效果,油汽比由0.13上升到0.15,为蒸汽驱后期合理的调整模式提供了借鉴。

     

    Abstract: In October 1998,steam drive pilot of 4 well groups are carried out in Lian Ⅱ layer of Qi-40 block.Steam drive expansive experiments of 7 well groups are carried out in July 2003.There are 11 well groups in steam drive area of Qi-40 block at present,which are all at the late development stage of steam drive breakthrough.Numerical simula-tion is applied to the late development stage of thermal recovery technology after water flooding to improve the eco-nomic efficiency of steam drive and to provide the adjustment of technology options for industrializing area.Injection temperature,injection rate and other parameters are designed to field show obvious effect.Oil-steam ratio climbed from 0.13 to 0.15,which provide a reasonable adjustment model for steam drive in late development stage of steam flooding.

     

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